Heathkit Troubleshooting Tips
Last updated: Thursday, 4 December 1997
Made some internal changes to speed up image loading and corrected
some of the obvious spelling errors. There's been no technical
changes since 29 March 97.
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I will update this information as necessary if I make any significant
changes to this file. --Bill
Introduction
From 1973 to 1978, I worked as an electronics technician at the Heathkit
Electronics Center (store #45) at 9207 Maple Street in Omaha, Nebraska.
It was the first "mini-store" that Heath Company tried. A mini-store
is a Heath store with three or less employees. A full-size Heath store
usually had eight or more employees. People in those stores could
be in sales or a specialized area of service.
In Heath's first mini-store, the three of us (that includes the
manager) did sales and service. Since I was more of a "techie" than
the other two, I spent most of my time repairing the products. (The
other employee, Vern, spent his time between TV repair and sales. The
manager, Joe, managed.)
Because we didn't have enough people to specialize, I ended up working
on a wide variety of Heath products. To help me keep track of the
problems associated with each product, I kept notes in a little
black notebook I purchased from Lefax®.
When I transferred to Michigan, I transcribed those notes to an H8
cassette and left a copy in Omaha for my successor. I was told that it
came in handy several times. Over the years, the tape had gotten
lost. However, I've managed to hang onto the original document and
have laboriously transcribed it again--this time for the Web.
Some words of caution: It's been a long time since I've
serviced Heath products and have forgotten a lot of the details of
some of the circuits described here. Though I've cleaned up some
of the grammer and spelling, I've left the original notes intact
if I could no longer recall what the note was about. The original
writing may make sense to an experienced technician still servicing
electronics.
Some of the fixes listed in here weren't authorized by Heath Company
and I doubt that they or anybody else will support them. They were
fixes that got the unit back to working within specifications and
back to the customer in a timely manner.
Also, many of these fixes are model number specific. What would
work for an SB-104, for example, would not work for an SB-104A.
So here's the
Legal Copout:
Don't attempt to use these service procedures unless you have a
strong background in electronics and can analyze the circuitry.
(I may have made some typographical errors when transcribing
this information and missed them during proofreading.) A
strong background in electronics would include attending a
two-year technical school, three years training and experience
with military digital electronics, a couple of mail-order courses
in computer and RF communications engineering, a First Class
Radiotelephone License with Ship's Radar Endorsement, and CET
certification. (What, me brag?)
In other words, don't blame me if applying these troubleshooting
tips gets you upset in some form.
With that bit noise out of the way, here's the notes from my little
black book. Have fun.
(By the way, I didn't single-handedly come up with all these ideas.
Many were suggested or inspired by others--or are factory-authorized
modifications. I just noted them down at the time. I'll try to
give credit where credit is due if I can remember who the contributor
is.)
--Bill
AA-Series Amplifiers
AA-22
- SPST pushbutton power switch breaks down quite often.
AA-29
- Hum and noise audible w/volume turned up and covers taken off:
This is normal (approx. 3mV @ 8 ohms measured with IM-48).
AD-Series Audio Equipment
AD-17, AD-19, AD-27, and Other Systems w/BSR-500 Changers
- Slow Speed and Slow Changer Action: Changer may even stop
during change cycle. Check idler wheel height adjustment. Replace idler
wheel if it has a "hardened" appearance. Clean idler wheel, pulley,
platter, and changer mechanism with a non-lubricating solvent
(Print-Kote®). Don't use tuner contact cleaner as it usually
contains silicon lubricant. Soak the bearing assembly in solvent
(the assembly at the base of the spindle). Lightly oil this
bearing assembly and the cam next to it after cleaning. Check
speed with a strobe disk. Clockwise movement of the markers
indicates a slightly fast rotation (normal). CCW movement is too slow.
(Contributed by John D'Amore, former Heath Field Service Manager.)
- Tone-arm won't clear raising pad, cuing lever operation jerky
(see Figure AD-1): At first appearance, it's the rising pad
(location 1), however, check the pivot screw (2) to make sure it isn't
too tight (this also has some effect on tone arm setdown).
- Tone-arm behaves normally halfway across LP, then
sticks--playing the same groove over and over. Manually moving
the tone arm inward about 1/2" fixes: This is due to grossly
misadjusted anti-skate adjustment, causing the antiskating spring
to latch on to one or more protuberances.
AD-17, AD-27
- Stylus #236-202 NLA. Replace entire cartridge, #236-201.
AD-27
- Parts for the turntable can also be found in the AD-17 manual.
AD-110
- Excessive meter deflection, left channel, in record mode,
w/recorder level turned up and service bulletin #AD-110-1 doesn't
help: Check C2. Place the banded end to ground. This is the
outer foil and provides shielding to prevent coupling from R66s bias
cable to C2. Also, reposition the wires from R34 as far from the
slide switch as possible (consider using shielded cable).
- Normal bias adjustment levels are about 25-28 Vrms at yellow wires of
head. Dropping to about 16 Vrms improves high frequency response but
causes distortion.
- The VU meters are used in record only--not playback.
AJ-Series Tuners
AJ-15
AJ-29
- No muting action: Check for leaky ZD-211.
AJ-33
- DPDT slide switches tend to open up or make intermittent
contact:
50-50 chance of being cured w/contact cleaner. Also, the clamps
holding the phenolic backs can be tightened.
AJ-43D
- The effect of the SCA filter switch is very obvious:
With this switch off, a high-pitched whistle can be heard in the
background on stereo programs.
AM Through AP-Series Audio Equipment
AN-2016
- Separation approximately 25 dB on Aux, Tape, and Tape
monitor inputs: This is normal. The coupling capacitance between
any disconnected unshielded input (or tape output) line to the rest
of the wiring harness measures about 30 pF.
AR-Series Receivers
AR-13
- Motorboats at turn-off: Check for bad C17-C18
(both capacitors are in the same can).
- Dim stereo lamp: Check for open C16.
- AM oscillations: High end too sensitive--back off the RF and
antenna trimmers to fix--will stay in specs.
AR-15
- 1 MHz oscillation at speaker output: Check 201 or 202
for leakage. Or miswired transistor sockets.
- AM or FM dial cord jams: Try repositioning the respective
tuning shaft bracket. As the tuning shaft is moved backwards,
there's less of a tendency to jam when rotating dial.
AR-29
- No mute function: Check for leaky ZD-211.
AR-1500
- Poor FM sensitivity: Check screw at coax ground lug on
tuner assembly. Should be 6-32 x 1/4". If 6-32 x 3/8", the screw
will short C802 (antenna trimmer) to ground.
- FM-IF DC voltage and relative RF levels: Set the FM signal
to about 100 mV, modulated w/1 kHz, deviation ? kHz at
88 MHz. Adjust the output to give an approximate level (RF) of
0.4 V p-p at IC-201, pin 6. Use a 10 MHz scope or better and a
low-capacitance X10 probe. This should show the following levels
(dc-volts w/vtvm):
Component DC Volts P-P RF (10.7 MHz)
--------- -------- -----------------
IC201-3 1.5 V 0.1
IC201-6 10.7 0.4
R202 0.2
Q201 base 1.0 0.2
Q201 collector 3.3 0.5
IC202-1 2.2 0.5
IC202-5 7.2 0.9
R210 0.3
IC203-1 2.2 0.3
IC203-5 7.0 2.5
T201-3 0.3 (audio)
- AGC and meter circuit levels. (Same setup as before.)
Component DC Volts P-P RF (10.7 MHz)
--------- -------- -----------------
Q204 base 0.7 0.5
Q204 collector 3.2 5.0
Q205 collector 12.3 7.0
R230, C228 -4.8 0
D201, D203 0 6 VAC (P-P)
D201, D202 0.8 0
R225 to meter 0.14 0
- Note: The previous two sets of measurements do not hold
true for the AR-1500-A model. In the "A" model, C220 was changed
from 0.05 uF (XC=0.2975 ohms) to 10 pF (XC=1.487
kilohms). This reduces the load on Q201s collector and a smaller
RF signal (0.1 V P-P) is developed at Q204s base. A smaller AGC
voltage is developed, so that the signal at Q201 collector is greater
(about 1.5 V P-P). Thus, for the same level of incoming signal, the
S-meter on the AR-1500A may indicate a lower level.
C-Series Automotive
CI-1079
- TI brand IC 443-7 may not always work here: Replace with
Fairchild brand 443-7.
CO-1015
- Cal position shows 2 cycles for a brief period:
Normal--can be speeded up somewhat by selecting D401 with a higher
reverse resistance.
- Non-linear sweep: Check for leaky Q402.
- Non-linear sweep: Check C401 by substitution (bad one gives
slight non-linearity but won't open eye of capacitor checker).
CO-2500
- Tachometer jitters: This is normal.
- Intermittent tachometer operation or no operation on motors other
than 8 cylinders: Check for spread sockets on pins 1 and 8 of
IC-203. If too heavy of wire is used during calibration, the
above may occur.
- TI brand IC 443-7 may not always work here: Replace with
Fairchild brand 443-7.
- Different balance voltages with modified board--R136 from 47 ohms
to 33 ohms. R123 from 22 kilohms to 47 kilohms.
E-Series Educational Products
ET-3400
- Intermittent or no display: Check for good ground at
IC6, pin 6.
G-Series Digital Clocks
GB-1201
- Count jumps a second or more when loading a number from
function 5 to function 6: Replace the rotary switch, SW3.
Be sure the insulation beneath it is installed. Note that the reset
button must be set in function 5 prior to counting up a number.
GC-1092
- One number brighter than others: Check D217 through
D223 for leakage.
- No DC-upverter operation after modification: Replace Q201
with a 417-233 (2N3643).
GC-1093
- Improved dynamic range for automatic dimming circuit:
Change R8 to 15 kilohms.
- Erratic operation: Make sure the customer
didn't use conductive foam tape (supplied with some clock chips)
for the padding between the crystal and the chip.
- Blue flare on AM or PM display: Check for leaky Q2--pulse
must be about 11 V P-P.
GD-Series Radio Control
(Note: If I remember right, I got most of the following
information from Bob Ellerton, who was a Heath Technical Consultant at
the time and an RC enthusiast. Later, he was promoted to Factory
Service Supervisor for the computer product line. Sometime after
that, he took over as Manager of the Heath User's Group.)
General
- Interference may occur when the receiver is installed
in the airplane, but not in the shop: This may be due to
metal-to-metal contact in the plane (push rods, etc.), rubbing
due to vibration and generating electrical noise
(see pg. 27 of GDA-1205-7 manual).
- Jittery Servos: This can be caused by the motor wiring.
If 180-degree rotation occurs, try reversing the connections
to the motor before replacing.
GDA-19-4
- Servos are sluggish or have poor torque: The
rack gears may be slightly out of tolerance. Also, observe
left-right pairing of rack gears (for proper centering).
- Sluggish in one direction, will rotate nearly 180 degrees
with servo simulator, centering standard causes rotation in one
extreme direction: All this is due to a dead monostable
multivibrator. Check that the red wire to C8 is wired to the center
tap and not the tap opposite the green wire.
GD-Series Small Items
GD-39
- Q10 should be 0.25 V saturated.
GD-48
- Marginal operation: Clean the search coil circuit board.
Check C6 for leakage. IT-28 "eye" should open in 5 to 10 seconds.
- Oscillator is temperature sensitive and may not work in extreme
cold or heat.
GD-113
- Intermittent oscillations in transmit: Tighten the
hardware to the switching board--the bracket--strap and solder
with braided shield if necessary.
GD-348
- Metal locator won't null properly, appears sensitive to the
shaft: This may be due to improper capacitance on the spiral
cable in the shaft. Try a capacitor-substitution box across various
combinations of points A, D, Y, F, and G on the audio circuit board
(if replacing the cable doesn't correct).
Placing a 0.02 uF ceramic disc (21-82) from "D" to "Y" on the audio
board on series #01306 corrected.
- Won't null: Check signal voltage drops across R106 and
R104. If no replacement search coil available, shunt R106 with
cap in the 12-25 pF range (such as 20-77 mica) (24 pf).
GD-1112/GD-1162
- Receives but won't transmit: Check Q1 (417-283).
Can be either of two types--bases and collectors reversed--see pg 22
of assembly manual.
GD-1150
- Normal Operation: No load draws about 0.3 to 0.4 amperes.
One inch of water with an object will draw 0.5 to 0.7 amps.
GDA-1158-3/-4
- 60 Hz modulation of the 40 kHz/56 kHz carrier (amplitude):
Replace Q102, Q103, and Q105 with 417-118s (2N3393). The B-1097s
that are supplied have a beta of >250 which appears to be the cause.
GD-1185
- Display won't blank when "E/R" pressed (step 11, pg. 82):
Check IC-1111. Measure IC-1111 with an IM-4100 and x10 probe
(PKW-101) in the "totalize" mode. X10 atten will normally read "8"
(E/R pressed), IC-1101 bad may read 16.
- Normal operating characteristics:
IC-1106-3: freq=1,733 kHz to 1750 kHz; pulse count=8 pulses
IC-1111-4: freq=108 kHz to 110 kHz; pulse count=8 pulses
IC-1111-6: same as IC-1111-4 except for a + or - 2 digit error
on the count.
GD-1187
- Do not use an isolation transformer--touch switch
may not work properly.
General Audio
Differential Power Amps
- Most Heath differential power amps (AA-1640, AR-1500, AA-29, etc.)
can be initially (and safely) tested by removing the load and output
transistors. The drivers should reproduce a waveform as it normally
would. If not, several expensive components have been saved from
destruction.
Tape Dubbing Test
- Tape Dubbing Test for New Audio Equipment: Plug a set of
stereo headphones into the dubbing input. Activate the dubbing switch.
Previous signal at the output should disappear. Turn the volume to
near maximum. Tap the left and right headphone. A faint tap should
be heard in the left and right speaker. Plug the headphones into the
dubbing output. Feed a signal into a function switch-selected input
(such as "AM" or "FM"). The signal should be faintly heard in the
headphones. Reduce the volume setting and return the system to normal.
GR-Series SWL and Ham Receivers
GR-78
- E-band dead on low end: (A) Replace Q301 with 417-167 (see
above). (B) Change R304 to 1500 ohms. (C) Change R303 to 2200 ohms.
(D) Swap L303 w/2200 ohms (prevents FMing when switching to "C" band).
- When aligning the unit, be sure the top cover is in place or
the C, D, E, and F bands my break into parasitic oscillation.
- E-band extremely touchy in alignment of the oscillator--both
high and low end: This can be caused by missing jumper wire from
SW-301B, pin 8 to the circuit board solder run (L305, R303, etc).
- Align the E and F bands first: If Q301 does not function
properly, it can be replaced without having to re-align the entire
unit. Do not attempt alignment without the top cover or the bottom
switch-board shield, or without the switch shaft installed. All
of these will affect the local oscillator frequency.
- E and F bands dead on the low end: This may be due to a
low gain-bandwidth product of Q301, so that with the lower Q of
C305-L305-R303 (on E) and C306, L306, R304 (on F) when tuned to
their respective low ends prevents enough positive feedback to
maintain oscillation. To cure, try removing R303 and replacing
the 2200 ohm at R304 with a 5600 ohm resistor. If this doesn't
work, try the unauthorized modification shown with the illustration,
above.
GR-110
- TI brand 443-7 will not always work here. Use Fairchild.
- Q101 and Q102 will measure 4 volts on gate two w/33 kilohm
resistors at R102 and R105 (used to be 15 kilohms).
- Priority oscillator won't "catch" channel "0" signal:
Replace IC-105.
GR-Series Television
GR-104
- Faint vertical bars: Check C232.
- High voltage drops with the brightness turned up--similar
to low horizontal drive: Check for open L201.
GR-300, 400, and 500
- No AFT: The AFT assembly may be installed backwards.
- AFC erratic; picture loses sync, picture polarity reverses:
Problem occurs when changing channels. Corrects itself when turning
the TV off or on: Check L327--should be to tuned to 2nd peak from
the top.
GR-900
- Luminance board #85-365-6 same as #85-365-9 except for Q254
in the dot generator and can be interchanged for most purposes.
- No 3.58 MHz from the oscillator circuit board but
the transformers and active components are okay: Check for an
open D406.
- Loss of interlace after 1/2 to 2 minutes of operation--sides
pull in: Waveform at pin 2 of horizontal oscillator board
about 2 V P-P sawtooth. Check for open L552.
- Boards check okay for any kind of problem, wiring appears
correct: Check the wiring harness at the breakouts. Now
and then, two or more wires will pinch together (possibly at
time of harness construction).
- No dots: Check for leaky C701.
- Intermittent horizontal jitter: Check C563.
- No AFT--adjusts okay: Check for reversed black and
red wires on red chassis plug.
GR-2000
- Preset tuning controls unable to adjust from low end of
Lo-VHF to high end of Lo-VHF (ditto for Hi-VHF): Check
collector voltages of Q201 through Q216. Only one should be high.
If not, the cathode voltages of D249 through D264 cannot be
properly controlled by any single tuning potentiometer. Outside
of bad solder connections or open transistors, check for
open/defective transistor sockets.
GR-2001
- Clock oscillation: (1) Put ferrite bead on Q53 collector.
(2) Change C114 to 0.001 on memory board of programmer.
H-Series Computers
H8
- Check for shorts between runs on the mother board.
Most common problem.
- +/-18 V supply failure next most common problem--possibly due
to improper board installation (mem & i/o).
- Female connector pins opening up is the most common cause of
intermittents.
- Due to H8 construction, address/data lines go low when asserted.
H8-1/3
- Distribution tape loads okay, but some functions won't work;
board passes memory tests: This can be due to bad RAM.
Swap IC's until symptoms change.
- 24K memory test: Set data at 040105 to 177.
Data Size
---- ----
057 4 K
077 8 K
117 12 K
137 16 K
157 20 K
177 24 K
217 28 K
237 32 K
257 36 K
277 40 K
317 44 K
337 48 K
357 52 K
377 56 K
64 K
- Memory test with WH-17:
See the note on memory testing the H17.
H8-5
- No 5-second pause prior to tape dump: Check the data
bus driver.
H8-16
- Memory test with H8-17:
See the note on memory testing the H-17.
- Passes memory test but I/O locks up after return key is
pressed when HDOS asks Action (BOOT): Check for faulty U117.
H9
- Cursor intermittently skips when typing: Place a 36 pF
(21-709) capacitor from S705-7 to ground on the TPU board.
- CRT displays random numbers, cursor moves backwards on 1st
turn-on: Try placing a 0.001 uF cap from IC738-13 to ground on
the TPU. (Contributed by Bill Sherman, former Heath Field Service
Manager.)
- Dim raster: Check for the presence of the CRT grounding
wire--also may be loose. (Contributed by Terry Bower, former
Heath TV technician.)
- Scan excessively wide: Check for leaky D307, D306, and D305.
- Pulses appear to be present, but unit still malfunctions:
Check the associated wiring harness--if a wire is open, other wires
will capacitively couple a signal over.
- Three cursors: Check for open P403-13.
- No Auto-carry defeat: Check for short to ground on S705-4.
- Cursor homes to lower right corner--won't advance--prints
character: Make sure P701 is plugged in.
- Cursor constantly moving: Check for open run to
IC734-5 (TPU).
- Column move to far right of page during Auto-carry and scroll
in short form: Check for open pin 8 on IC528.
- Cursor won't home after transmit page: Check IC513.
- Page filled with "?": Check for open write-enable line.
- Cursor skips spaces in a "binary" manner: Check for shorts
between pins 9, 10, 15, and 16 of cursor latch IC501.
- No scroll: Check for interchanged blue and green wires
to S503-5 and -6 beneath the picture tube. Green should go to S503-5.
- P603 pin-out (rear view):
- 20 mA current loop (passive):
- I'm not sure how I used the above circuit to test the H9
20 mA passive current loop function. Apparently, I plugged the dual
bananna connector into a 20 VDC power supply and did something with
the switch. The switch may represent a keyboard key and pressing
it would echo the character back to the screen. (ww 6 July 1996)
- Cursor advances only 10 spaces and then returns to the
beginning of the line: Check for data flow from IC-502 to
IC-504B to IC-509.
- Only character displayed is at the upper left corner--cursor
won't advance: Check for a short circuit between S502-1
(cursor latch enable) and S502-2 (select scroll divide-by-12)--on
the top of the chassis below the CRT.
- NOTE: Many of the problems in the H9s were due to the
fact that the spring connectors on the factory-built wiring harness
were pinched onto the wires rather than soldered. If you're
attempting to restore one of these terminals, you may need to remove
the connectors from their shells and solder them. (ww 30 June 96)
H10
- Drops or adds an occasional bit of data (reader): Be sure
that the retainer beneath the tape lamp is flat against the bottom
of the tape guide. Check that the bulb filament is horizontal and
directly above the reader holes.
- Drops or adds bits of data--reader/punch: Be sure the
power supply switch is in "normal." Also check that the slide
from the reader slot is low enough that fan-fold paper
tape won't catch on the top--causing the sprocket to momentarily skip.
- NOTE: When punching tape, the solenoids in the early
H10s would tend to jam and tear the paper tape. This was because
they would heat up and the shafts would warp. Heath Company fixed
this by changing to a more reliable part. Sorry, I have no memory
of what the part numbers are. (ww 30 June 1996)
H14
- Passes initial test, intermittently passes initial "on line" test
but print head only moves back and forth continuously with all ICs
installed and the on-line button pressed: Check for a short
between data lines D6 and D7.
H17
- Motor clatters: Check for a short circuit between
U8A-3 (writegate-low) and U7B-3 (readdata-low).
- Memory can be tested by using the program at 030 003A in PROM:
(A) Set PC=030003
(B) Press "Go."
The HL registers now contains the starting address 040100A.
The DE registers contain the ending address--64 bytes below the
stack pointer location in upper memory. If desired, both can be changed.
(C) Monitor the B register.
If a failure occurs, the B register contains the byte that failed
while the HL register points to the address that failed.
- AT: address: 374Q
- No I/O response after Return key is pressed for "Action (BOOT)"
prompt: Check for a faulty U117 on the H8-16 board.
H27
- Door assembly replacement: #969-34 (G-288, Dec. 22, 1978).
- Complete drive part number: #150-73.
H-Series Ham Equipment
HD-1982 and HW-2036
- 5 kHz deviation adjusts to about 11 o'clock as seen from the front.
Setting the micoder level will then give about 2 kHz deviation at
9 o'clock.
HD-1982 and HWA-2021-3
- The LEDs appear to be heat sensitive and may be destroyed easily
with a too-hot of an iron. Use a heat sink.
HG-10B
- The key jack in the back of the unit is used only for cathode
keying--see page 32 (Operation) and page 28, 1st paragraph.
HM-102, HM-103
- The wattmeter portions are usually tuned for 7 MHz (40 M). For
other frequencies, a correction factor curve should be calculated
using a dummy load, RF probe, and VTVM. The equation is:
P=E2/R
HM-2102
- SWR won't null: This is due to too much capacitive
loading to the brass eyelet from L1. Remove C16 and the brass
eyelet (in extreme cases).
HN-31
- To prevent accidental oil spills: Use 1 part mineral oil to 4 parts
paraffin (melting point about 135oF). (This is either from
a factory modification, or I'd seen it in some trade journal. I've
never tried it myself. --ww 8 Jul 96)
HR-10B
- No AVC, no S-meter movement with received signal: Check
terminal strip A (pg. 1, pict. 15). May be installed
backwards. (A service bulletin covers this.)
HR-1680
- Check for missing 3900-ohm resistor on the power supply board.
- Pre-selector oscillates: Adjust pre-selector wires with
50-ohm non-reactive load on the antenna.
HW-8
- Won't tune: Q11 may be installed backwards.
HW-16
- A quick and dirty technique to check over-all receiver accuracy
and 80-meter sensitivity is to tune to 3.579545 MHz using a short piece
of wire for an antenna. If there is a color TV operating nearby,
the receiver should be able to pick this up and zero-beat to it.
HW-32
- It's normal for there to be as much as 3 dB power difference
between the USB and the LSB.
- Normal power output is 25 to 50 watts (power appears to be
higher on LSB and low end of band).
HW-32A
- Relay chatters in VOX mode: Remove C203.
HW-100
- Instability: See service bulletin GH-1, dated July 10, 1968.
- Audio pre-amp and VOX info: See bulletins #GH-3 (July 7, 1969)
and GH-2 (Aug 20, 1968).
HW-101
(A couple of these are my own, but most came from Engineering,
Tech. Consultants, Heath technicians, and field technicians.
The HW-101 was a great transceiver, but it was truly an art to
repair one that was broken.)
- Receive audio amplifier oscillates with RF gain set to
2 o'clock: Check for open R323 at V14A.
- No RF out: Check for interchanged R938 and R916 (near
V9 and V8).
- R14 and R112 cooked: White-blue and White-blue-blue
wires on RL-2 may be interchanged.
- R223 and R109 cooked: Check for short across C111.
- RL2 keys after warm-up: Check for leaky D202 at V12B (56-25).
- Low power output: This is affected by the placement of the
grounds on the shields in the HFO stages. The rear shield is the most
critical. Remove the "fingers" on the rear shield cover. The
power can be tuned for maximum output by properly positioning the
grounding solder.
- Microphonics on receive calibrate: This is normal if they
occur when the unit is jarred.
- 7 MHz and 14 MHz (40 & 20 meters) bands dips instead of peaks
(rcv & xmit): This is the combined effects of L702 through L705
and/or L802 through L805. Selecting coils for the offending board
may help. In one case, the culprits were the 21 MHz (15 meter) coils.
- Low power output, all bands, worse on 10 meters: Try
replacing the finals (V8, V9) with GE-brand tubes.
RCA-brand tubes appear to be the cause. Also, sub V7.
- Low power output at 40 meters: Check C703, C704, C802,
and C803. May be out of tolerance.
- Oscillates on 15 and 10 meters: Be sure that the
neutralization wire from the preselector isn't shorted to ground.
Check for good grounds on the shields of the drivers.
- Relay chatter in VOX mode: Replace the two wht/rd/rd
wires to R213/R214 with shielded cable. Ground the shields near
R213/R214.
- High plate current, no RF power out on some bands--receive
okay: Check for broken taps on L904.
HW-2021
An anecdote: In 1979 I was promoted from Senior Technician to
Service Technical Writer and was transferred from Omaha to
St. Joseph, Michigan. There was kind of a fire going on and I was
required to write service manuals on the newly released
H19 terminal and H89 computer.
After I finished them, my boss, Frank K., assigned me
to write a manual on a new Heath 2-meter handy-talky. (I no longer
remember what the model number was.) Frank advised me to
use the HW-2021 service manual as a guide. I, with
my vast experience of writing two service manuals, pointed out
to him that while the HW-2021 manual was good, I found it
lacking. I went on at great length describing in detail how I
could write a better manual.
When I finally stopped to catch my breath, Frank quietly said "I
wrote that manual."
Meanwhile, our typist/proofreader/illustrator, Fran, was doing
her damnedest not to bust a gut.
At the time, I didn't realize that I was still new and that Frank
had many more years of servicing, writing, and editing experience than
I did.
Frank was okay, though. You begin to realize you have a good boss
when you work for him for 13 years and even turn down job offers
from other departments.
- TVI: May be due to 45 MHz radiation. Disconnect the brown
wire from hole "U" on the main circuit board and reconnect at the hole
near the emitter of Q15.
- The collector VRF of Q24 is normally lower than that
of the collector of Q23. Other stages show gain.
- Low power output: Make sure that the P.A. transistor is
mounted close to the board.
- Offset switch damage occurs easily, check while servicing.
- Quieting is normally best about 1 kHz below minimum THD.
- Oscillator won't net: Change C57 to 56 pf. Also try
changing the netting capacitors or the bias resistors to the
varactor diode (in extreme conditions).
- Receive oscillations: Check for a well-grounded clip
at the antenna terminal. Build up a layer of solder on the foil-side
screw-hole rings on the circuit board to insure a good ground
connection to the metalized plastic case. To give a better
ground contact for the antenna, place the flat washer
on the antenna jack on the inside of the case.
- Batteries won't charge: Check the spring assemblies in the
battery pack. These can protrude and short to the case.
- Transmitter alignment: Be sure the power supply voltage
to the transmitter circuits are the correct levels. Either use
the battery pack or increase the external DC supply to the point
that equals normal battery pack operation. Otherwise, you'll get
erratic results.
- 1 mH chokes (#45-80) are heat sensitive and can easily be
destroyed.
- Erratic oscillator: Look for the 1 mH in the
??? circuit rather than the circuit of Q???.
HW-2026
If I remember right, the HW-2026 caused some serious cross-talk
problems in cities with repeaters that were close together.
At the time, the Heath engineers could not solve the problem (short
of totally redesigning the unit). So the Heath company contacted all
their customers to recall the kit. The deal was this: If the kit
wasn't built yet, Heath would refund the customer's money plus
pay an extra $25. If the kit was already assembled, Heath would
refund the money plus pay the customer $50 (big bucks in those
days). If the customer chose not to return the kit, Heath would not
provide service or any other support.
Amazingly, many customers chose to keep the radio.
- Its spurs were -40db @ +/- 2 MHz of the carrier. The HW-2036 is
-70db at +/- 20 MHz of the carrier.
HW-2036
- Excessive spurs on 146.84 MHz and 146.76 MHz. Buries the
needle with the cover on: Check L202 for proper installation.
- Receiver spurs on 146.00 MHz, 147.00 MHz, and 148.00 MHz:
Adjust C144 for 10.000775 MHz at TP-108. Y405 for 21.54934 MHz,
"-600 kHz" for 23.23323 MHz. "Sim" for 23.33323 MHz and "+600 kHz"
for 23.43323 MHz.
- VCO won't lock above 147.5 MHz in XMT in cold weather:
Check for faulty C416 (#215-221).
HWA-2021-3
- The pushbuttons must be pressed firmly or only one tone
may be generated.
HX-20
- Normal operating characteristics: There should be no
carrier transmitted when the Mode and Audio Gain
are switches in the CW position and the
Standby-Spot-Operate switch is in the Operate
position. If there is, check the carrier null. If CR1/CR2 is
defective, replace with 56-87s.
- RF output is 50 watts up to 10 meters, which is about 25 watts.
- Finals may oscillate on an antenna with an SWR >2:1.
I-Series Counters, Generators, and Meters
IB-1103
- First digit counts up. All others are zero: Check
the reset pulse amplitude at Q102. If low, replace Q102.
- Multiplier doesn't work: If correct frequency is applied
and unlock lamp goes out, suspect IC509. If no IC509 in stock
(#443-624/MC1023P), substitute IC501 out of the AJ-1510 (443-38)
which is a MC1023P selected for tighter parameters.
IG-28
- Excessive bend in vertical lines at top of screen with
signal being injected through tuner--present mods don't help:
Install the following change:
IG-42
- If the selenium rectifier should fail, a 600 PIV, 1 ampere diode
(#57-27) in series with a 0.1 to 0.125 ampere slow-blow pigtail fuse
will substitute.
IG-57A
- Marker ripple: Normal. See page 59, column 2.
IG-1271
(Most of this is based on information from an article written
by Charles Gilmore (who was a Heath engineer at the time) in the
May, 1976 issue of Radio Electronics.)
- Slew rate: The maximum rate of change that the
voltage-controlled generator can be varied.
- VCG linearity: The degree of match between the theoretical
frequency of the generator and the actual frequency caused by the
controlling voltage. Expressed as a percent of maximum control
voltage.
- It is possible for the amplitude in some generators to drop as
much as 2 dB when switching from the lowest frequency sine wave to the
highest. This roll-off is due to filter circuits in the output
amplifier. (The filters are used to eliminate distortion due to
high-frequency spurs in the synthesized sine wave.)
- The low-impedance output (50 ohms) is used to reduce line
reflections and maintain good square waves.
IM-17
- Meter won't zero after installing modification #IM-17-2:
Try selecting Q1 and Q2 for matched gains (gm).
IM-18
The IM-18 VTVM was one of my favorite tools. It was one of those
basic designs that couldn't be improved upon. The circuitry was
essentially the same since it was introduced (under a different
model number) back in the '50s. The circuitry hadn't changed in the late
'70s when it was later given a new paint job and the model number changed
(Marketing moves in mysterious ways).
Anyway, it was a rugged tool. In the '70s, Heath came up with an
upgrade (the IMA-18-1) that replaced the two vacuum tubes with
solid-state equivalents so that it would be ready the instant you
turned it on. I did a lot of warranty service on the modified
units as they tended to blow up when brought near the high-voltage
circuits in color TVs. I think most customers who bought the mod went
back to the vacuum tubes.
- Needle pegs on DC or AC on first turn-on: Suspect a leaky
DC-cal or AC-cal potentiometer.
IM-25
- AC bias won't adjust to 6 volts: Replace C7 with #25-220
tantalum capacitor. The original component was a standard electrolytic,
which would get leaky after a couple of year's operation.
IM-48
- Meter needle jumps around as if indicating intermittent noise:
Replace the twin triode, 12AT7. It's developed an intermittent short
or leakage. This usually happens after about 2000 hours of operation.
- False distortion readings: Back off the amplifiers level
controls as the 12 dB ratio (1 V & 0.25 V) at the input may be
overdriving it. Problem may also be due to ground loops--remove
grounds.
IM-104
- Needle pegs--battery test okay: Check the batteries.
Burgess types have recessed negative terminals and may not make
proper contact (left side, facing back of meter).
- Fine-zero adjust won't adjust down to zero after R37
is set to 0.6: The position of the 0.1 CAL control may be off.
Also, check R37, may be out of tolerance (too large in value).
IM-1202, IM-1212
- Oscillator won't adjust properly: Check the input wiring.
Change R208 to 8.2 kilohms.
IM-1210
- Counts randomly, zero adjustment won't adjust for 00 on
DDV set-ups (pg 42, col. 2, step 3): Check for open voltage
divider string.
- Zero adjustment won't adjust properly: Check for R14
or R17 (22 megohms, red-red-blue) interchanged with R56 (6200 ohms,
blue-red-red).
IM-1212
- Reads zeros--faint count in the background: This is due
to noise on reset line of IC6 and IC7. Shunt R217 with a 0.005 uF
disk capacitor (#21-46).
IM-2202
- Display doesn't flash properly in Battery Test; other modes
okay: Check for shorted D202.
- Metal sleeves tend not to make contact under the switches.
Quickest fix is to run jumper wires. For example, a jumper wire
can be run from the hole near "AG" to its appropriate tab on "G" of
the rotary switch (on the foil side of the board) and fed to its
appropriate position on the push-button switch.
- Low or nonlinear AC readings: Check for open C103.
IM-4100
- No clock: Check for missing +VCC jumper wire to
clock IC (next to crystal).
- D105, G-segment is on constantly: Check for short from wire
connection "E" to +VCC-side of R102 (component side of board).
IM-5248
- False distortion readings: See the note under
IM-48 in this file.
IM-5284
- Red wire: AF-AB.
- Black wire: AA-AC.
IMA-18-1
- 6AL5 = TR1002 = #150-57
- 12AU7 = TR1119 = #150-58
IO-Series Oscilloscopes
Oscilloscopes are cool. I could sit and watch waveforms all day.
IO-101
- Excessive bend in vertical lines at top of screen with
signal being injected through tuner--present mods don't help:
See the modification for the IG-28.
IO-104
- The brightness adjustment range is strongly dependent on the line
voltage. At about 130 VRMS, the trace may not totally
blank.
- 60 Hz modulation on the Z-axis: Check the positive and
negative regulation zeners in the high-voltage circuitry.
- Normal operating characteristics: The trace will drift
vertically during the first hour of warm-up. Also, it's normal
for the trace to trigger on different levels when switching from
"Auto" to "Norm."
IO-4510
- Auto-baseline intermittently disappears with trigger-select
on one channel at 2 ms/cm, but not other (usually Y2): Normal.
IO-4530
- Vertical position control moves trace only 1/2 screen:
Check R27 (vert. cal.) adjustment first.
IO-4540/IO-4560
- Trace shortens on left at fastest sweep speed: This is
due to a misadjusted sweep calibrate control (internal).
- Vertical position shifts at different sweep speeds: This is
due to the fact that the power supplies are unregulated.
IO-4540
- Sweep shortens on left on lower sweep speeds (auto-baseline):
Try substituting IC-304.
IO-4550
- Time/cm won't range properly, variable control has little or
no effect: Check Q204--may be extremely leaky or shorted.
- No trace on initial turn-on: Check adjustment of sweep
length and calibrate controls.
- Crosstalk: Check the lead dress of the wires from Q117-1
and Q117-2. Match the betas of Q107 and Q108--preferably 140 or
greater.
- Horizontal oscillation on low sweep speeds: Try replacing
Q210 (#417-235).
IO-4555
- Trace moves vertically when position knob touched: Q109-2
and Q110-2 may be interchanged with Q107-2 and Q108-2.
- Low frequency horizontal jitter: Position the scope so that
it's facing you and is right-side up. Next, route the white/red
wire from "BC" (horizontal sweep) over the timebase switch.
- Trace blanks in the X-Y mode: Clip pin 13 of IC209.
M-Series Marine Equipment
MI-Series Depth Sounders
(I think this information came from either John D'Amore or Kent
Barnes--both Field Service Managers at one time or another.)
Second and third echos at high sensitivity levels are due to the
transmitted signal being re-reflected from the air-water junction,
to the lake bottom, and back up again. When calibrating depth sounders
for peak output and greatest sensitivity, first adjust for maximum number
of multiple echos, then reduce the sensitivity to minimum and try for
a second echo.
MI-29
- Will not properly test on the FS-1 Fish Simulator due to the
fixed-width return pulse: It gives the effect of a shifting depth
as the noise-reject control is adjusted. Normal.
- To date, the highest failure-rate component is also the most
expensive--the motor at $22.00.
MI-2900, MI-2901, MI-1030, and MI-1031
- Out-of-water sensitivity check: Carefully aim the transducer
at a hard surface (a cement floor). Aiming is critical--try for
90o. With the sensitivity full clockwise and the transducer
about four feet away from the surface, an echo should occur at about
the 10-15 foot depth.
- Note: The above will not work for the transom transducer.
The dispersion angle is different.
MI-1030, MI-1031
- Checking sensitivity: Short the base of Q8 to ground to
kill the transmitter. Connect a signal generator to the output
(transducer disconnected) through a 0.1 uF capacitor. Set the
signal for about 80 uV at 30% amplitude modulation. Turning the
MI-1031 sensitivity control 1/2-way up should show flashes around
the display (for a 1000 Hz modulating signal).
MP-10
- If a power transistor shorts, replace both. Beware of
Sylvania ECG179 substitutions.
Parts
45- 80-00 heat sensitive
417- 264-00 may sub for 417-818
432- 72-00 subs 432-861
Probes
PKW-101
- Compensated scope probe. DC to 60 MHz. Input impedance is 10 megohms
and 11.5 picofarads. Compensation for 1 megohm/15-10 pF scope
input. X10 attenuation. 500 VAC & DC rating. (1 megohm with
35 pF shunt for IO-105 to 1 megohm shunted by about 40 pF in the
IO-4510. This is about the same for Heath frequency counters, also.)
This type of probe is also good for frequency counters as it has
built-in circuits to prevent ringing.)
- Common frequency input impedances:
Frequency XC
--------- -------------
10.7 MHz 1293 ohms
455 kHz 30.5 kilohms
3.395 MHz 4 kilohms
15.75 kHz 880 kilohms
SB-Series Ham Equipment
SB-100
- "Pop" heard in receiver. Intermittent changes in receive
level after warm-up. S-meter affected, but transmitter may be okay:
Check AVC tube V13 (6BN8).
SB-104
- ALC deflects upward when the tun button pressed and MIC/CW
level full CCW: Check ZD-301 with an IM-18 on Rx1Meg.
Reverse resistance should be greater than 1 megohms. If a #56-59
isn't in stock, substitute a #56-44 using the above selection
procedure.
- Normal operating characteristics: Peak "tune" power at
about 11 o'clock to 12 o'clock. Voice peaks on wattmeter should be
about 10 watts on relative power meter (from "3" to "6"). ALC
meter indication may be lower and erratic. Newer kits will be lower
still due to R621 on the "E" board (carrier generator) being
changed from 22 ohms to 100 ohms.
- High-power PA oscillations: Check continuity from phone
plug shields to coax cable shields on PA and ALC boards.
SB-303, SB-313
- IF oscillations: Check that the coaxial cable from the BFO
has its shield soldered to point "J."
- IF oscillations: Check the grounding of the IF cans.
Reposition the metal strip so that it contacts these cans.
SB-634
- To test Null on the phone patch, set the IG-18 to 800 Hz and
connect it to the RCVR input and place a 600-ohm load on the
Phone Lines connector. Place "Mon/Null" to "Null" and make the
null adjustment.
- Extreme flicker on X1 seconds and X1 minutes when displaying
1s and 7s: Change IC-201 to #443-601, R237 to 15 kilohms (#1-21),
and C201 to 30 pF (#20-100).
SW-717
- Oscillation on high end of "D" band: Try replacing C24.
All parameters may test good, but replacing will cure.
- Weak audio; distorted: Shunt C24 with a 0.22 uF to
0.39 uF capacitor.
- Main tuning dial stiff: Add a lockwasher to the brass
bushing. Lightly oil the brass bushing and add silicon grease to
the dial pointer.
- Bandspread dial slips moving from left to right: Loosen
the tension on the spring by stretching it slightly.
T-Series Equipment
TD-1080
- Only one or two notes are produced: Check for a leaky
on D3 through D18.
- Notes present, but weak: Try subbing Q7 and Q8 (#417-235
and #417-801). This circuit is critical.
- Notes present, but weak: Check Q5. Pulses on Q6 are
extremely sharp.
Those are my notes.
I have no plans to adding to them (other than correcting errors I've
missed). This is partly because I want to use the remaining space on
this URL for other projects. If you have a collection of service
hints for Heath products (or other Heath information) that you want
to share, place them on your Web page, please
email me and I will create a link to your page.
--Bill
Return to the Heath Company page.
Copyright © 1996, 1997, William A. Wilkinson. All rights reserved.
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